Failure investigation of super heater tubes of coal fired power plant
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This report discusses the analysis of the failure that occurred in two adjacent super heater tubes that were made up of CrMo steel in a 60 MW thermal power plant that made use of coal. It proposes a risk mitigation strategy as well.
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Running head: RISK MANAGEMENT
[Risk Management]
[Name of the Student]
[Name of the University]
[Author note]
[Risk Management]
[Name of the Student]
[Name of the University]
[Author note]
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2RISK MANAGEMENT
Failure investigation of super heater tubes of coal fired power
plant
[Name of the Student] [Student ID]
1. Introduction
The report mainly discusses about the analysis of the failure that occurred in two adjacent super heater
tubes that were made up of CrMo steel. This was a 60 MW thermal power plant that made use of the
coal. The major reason lying behind the failure was due to the oxide deposition upon the internal
surface of the tube and this deposition was initially responsible for the creation of a significant
amount of resistance for the heat transfer process [1]. This in turn was associated with undesirable rise
in the temperature of the components. Besides this the report has also been associated with proposing
the risk mitigation strategy as well.
2. Research and Theory on the Problem
2.1. Specific Theory – In a power plant the prime importance is provided to the process required for
the purpose of generating electricity without the existence of any kind of forced outages. The major
concern for the forced outages in the coal fire station is due to eh failure of the super heater tube of the
boilers. The major reason lying behind the damage occurring over the time of operation is due to the
flowing of the fuel gases over the super heater tubes. This type of damage is often termed as the
fireside damage or corrosion. This type of damage is generally dependent upon the coal quality, as
well as on the materials that are being used along with the various operations and the maintenance. It
is seen that the tubes interior is generally vulnerable and are primarily dependent upon the water
quality that is used for the generating steam of high pressure [2]. So there is an essential need of a
steady or continuous flow of steam so as to make sure that the materials of the tube are maintained
under the temperature that has been prescribed. In case of its absence there exists the high possibility
of shooting-up of the temperature which in turn is responsible for the detrition of the materials as well
as the subsequent failure at a fast rate. For such instances the overall efficiency of the plant is entirely
dropped. So it is very essential to analyse the failure of the tubes in order to find as solution for taking
certain actions that would be helping in avoiding such kind of risks in the future [3].
2.2. Specific Theory – Risk and Management
The possible ways that are to be adopted in order to eliminate the further risks similar to the boiler
incident have been listed below:
Failure investigation of super heater tubes of coal fired power
plant
[Name of the Student] [Student ID]
1. Introduction
The report mainly discusses about the analysis of the failure that occurred in two adjacent super heater
tubes that were made up of CrMo steel. This was a 60 MW thermal power plant that made use of the
coal. The major reason lying behind the failure was due to the oxide deposition upon the internal
surface of the tube and this deposition was initially responsible for the creation of a significant
amount of resistance for the heat transfer process [1]. This in turn was associated with undesirable rise
in the temperature of the components. Besides this the report has also been associated with proposing
the risk mitigation strategy as well.
2. Research and Theory on the Problem
2.1. Specific Theory – In a power plant the prime importance is provided to the process required for
the purpose of generating electricity without the existence of any kind of forced outages. The major
concern for the forced outages in the coal fire station is due to eh failure of the super heater tube of the
boilers. The major reason lying behind the damage occurring over the time of operation is due to the
flowing of the fuel gases over the super heater tubes. This type of damage is often termed as the
fireside damage or corrosion. This type of damage is generally dependent upon the coal quality, as
well as on the materials that are being used along with the various operations and the maintenance. It
is seen that the tubes interior is generally vulnerable and are primarily dependent upon the water
quality that is used for the generating steam of high pressure [2]. So there is an essential need of a
steady or continuous flow of steam so as to make sure that the materials of the tube are maintained
under the temperature that has been prescribed. In case of its absence there exists the high possibility
of shooting-up of the temperature which in turn is responsible for the detrition of the materials as well
as the subsequent failure at a fast rate. For such instances the overall efficiency of the plant is entirely
dropped. So it is very essential to analyse the failure of the tubes in order to find as solution for taking
certain actions that would be helping in avoiding such kind of risks in the future [3].
2.2. Specific Theory – Risk and Management
The possible ways that are to be adopted in order to eliminate the further risks similar to the boiler
incident have been listed below:
3RISK MANAGEMENT
The tube wall are to be cleaned at regular intervals in order to avoid similar incidents. The regular
checking would be helping a lot in detecting any kind of defects if occurs before any kind of
severe consequences. This would be helping a lot in removing all the hindrance or the
heterogeneities as well [4].
One major thing that is to be done is checking the quality of water. This is to be done at regular
intervals. The major reason behind doing this is for the purpose of making sure that all the pH and
the oxygen level is maintained at specified levels.
Another problem which might occur is due to the contamination of the water. This mainly occurs
due to the leakage in the tubes that might lead to high salt concentration in the water. By regular
monitoring it is possible to eliminate this kind of risk as well.
The strength of the materials are to be checked as well so as to eliminate the risk of the thickening
of boundary walls [5].
Maintenance of the oxide scale so as to make sure that there is smooth heat transfer that would be
helping in the elimination of risks related to overheating of the tube walls.
All this things are to be maintained in order to eliminate the risks related to bulging which mainly
occurs due to high hoop stress that might be leading to failure.
3. Link between Case Evidence and Theory
The damage of the tubes were visible with naked eyes only. It was observed that both of the tubes
were associated with experiencing a temperature of around 540 C and was associated with a stress
level of around 100kg/cm2 at the time of operation. In one of the sample it was observed that there
existed fish mouth cracking I one side whereas on the other side of the welding there was a bulge.
Besides this there also existed a layer wise corrosion at the open end of the crack [6]. Besides this
there existed a drastic decrease in the thickness of the walls as well. There also existed multiple cracks
in the inner surface in the longitudinal direction but this type of cracks were entirely absent in the
outer surface. So it was observed that the outer surface was blackened that lead to thermal effect
whereas the inner surface was entirely deep brown in colour having multiple red spots.
Some of the facts that were identified after analysing the entire incident have been listed below:
Cr-Mo low alloy steel was used for the purpose of making the component and besides this the
composition was very much close to the specification of the polish. Some of the specifications
mainly includes the DIN 10CrMo910/T22. Besides this it was also observed that the major
chemical concentrations were within the limit that was specified previously.
It was seen that there existed polygonal fertile grains as well as alloy carbide in the
iMicrostructure of the steel tube. At the time of service exposure there occurred the formation of
oxide scales in the interior of the tube. During the time when it was observed that the thickness
become substantial then it was time when the process of heat transfer was hindered all across the
The tube wall are to be cleaned at regular intervals in order to avoid similar incidents. The regular
checking would be helping a lot in detecting any kind of defects if occurs before any kind of
severe consequences. This would be helping a lot in removing all the hindrance or the
heterogeneities as well [4].
One major thing that is to be done is checking the quality of water. This is to be done at regular
intervals. The major reason behind doing this is for the purpose of making sure that all the pH and
the oxygen level is maintained at specified levels.
Another problem which might occur is due to the contamination of the water. This mainly occurs
due to the leakage in the tubes that might lead to high salt concentration in the water. By regular
monitoring it is possible to eliminate this kind of risk as well.
The strength of the materials are to be checked as well so as to eliminate the risk of the thickening
of boundary walls [5].
Maintenance of the oxide scale so as to make sure that there is smooth heat transfer that would be
helping in the elimination of risks related to overheating of the tube walls.
All this things are to be maintained in order to eliminate the risks related to bulging which mainly
occurs due to high hoop stress that might be leading to failure.
3. Link between Case Evidence and Theory
The damage of the tubes were visible with naked eyes only. It was observed that both of the tubes
were associated with experiencing a temperature of around 540 C and was associated with a stress
level of around 100kg/cm2 at the time of operation. In one of the sample it was observed that there
existed fish mouth cracking I one side whereas on the other side of the welding there was a bulge.
Besides this there also existed a layer wise corrosion at the open end of the crack [6]. Besides this
there existed a drastic decrease in the thickness of the walls as well. There also existed multiple cracks
in the inner surface in the longitudinal direction but this type of cracks were entirely absent in the
outer surface. So it was observed that the outer surface was blackened that lead to thermal effect
whereas the inner surface was entirely deep brown in colour having multiple red spots.
Some of the facts that were identified after analysing the entire incident have been listed below:
Cr-Mo low alloy steel was used for the purpose of making the component and besides this the
composition was very much close to the specification of the polish. Some of the specifications
mainly includes the DIN 10CrMo910/T22. Besides this it was also observed that the major
chemical concentrations were within the limit that was specified previously.
It was seen that there existed polygonal fertile grains as well as alloy carbide in the
iMicrostructure of the steel tube. At the time of service exposure there occurred the formation of
oxide scales in the interior of the tube. During the time when it was observed that the thickness
become substantial then it was time when the process of heat transfer was hindered all across the
4RISK MANAGEMENT
walls of the tube [7]. This initially led to the localized heating. Besides this the formation of the
scales along with the growth as well as the subsequent removal due to the loosening from the
materials surface occurred as a continuous process. Initially this was responsible for the reduction
in the thickness of the tube walls. Despite of all this there was the condition when it entered the
non-steady state phenomenon and along with this any kind of future quantification of the data
would be associated with misleading of the information related to the high temperature
deformation characteristics. In addition to this the heating was associated with the coarsening of
the carbidesand was also responsible for propelling of the perception of the new brittle phases
along with the boundaries of the grain. This was further responsible for the embrittlement [8].
Facing excessive amount of stress as well as high temperature the sliding of the grain boundaries
initially promoted the formation of void all along the boundaries and initially at the latter stage
they were interconnected with each other leading to the weakening of the structure[9].
Besides this there was a drastic change in the dimensions of the tube near the fracture and it
looked like the materials of the tube got softened at an extreme rate. The evaluation as associated
with further confirming of the material softening and this evaluation was generally done upon the
bulk hardness that was observed near the location which failed. The values that were obtained was
seen to be exorbitantly law when compared with the materials that were investigated. Additionally
the earlier effect of the formation of the scale, and besides the softening was also responsible for
effecting the flow of the materials along with the creation of the bulge.
The inter-granular cracking along with the subsequent overloading of the ductile fracture under
excessive amount of hoop stress that was beyond the yield point of the tube material initially lead
to the failure at the time of exploitation of the service [10].
4. Solution
The most possible ways by which this kind of failures can be eliminated is by proper monitoring of
the entire process. Everything needs to be monitored in a proper way along with which proper
materials are also to be used of the purpose of creating a proper tube of the boilers which are essential
for the purpose of eliminating this kind of the problems. Besides this there is also a need of proper
cleaning as well so as to eliminate the formation of oxides as well as the subsequent spilling from
inside the tubes wall. Besides this good quality water should also be used so as to prevent thickening
of the walls [11]. Creep and softening of the materials is another problem that was responsible for the
failure. Oxide scale management would be helping in the smoothing of the heat transfer process
initially helping in the elimination of local overheating. Besides the steam pressure is to be decreased
at a substantial rate so as to decrease the stress occurring due to high temperature creep. This would
be helping in preventing the softening of the materials as well.
walls of the tube [7]. This initially led to the localized heating. Besides this the formation of the
scales along with the growth as well as the subsequent removal due to the loosening from the
materials surface occurred as a continuous process. Initially this was responsible for the reduction
in the thickness of the tube walls. Despite of all this there was the condition when it entered the
non-steady state phenomenon and along with this any kind of future quantification of the data
would be associated with misleading of the information related to the high temperature
deformation characteristics. In addition to this the heating was associated with the coarsening of
the carbidesand was also responsible for propelling of the perception of the new brittle phases
along with the boundaries of the grain. This was further responsible for the embrittlement [8].
Facing excessive amount of stress as well as high temperature the sliding of the grain boundaries
initially promoted the formation of void all along the boundaries and initially at the latter stage
they were interconnected with each other leading to the weakening of the structure[9].
Besides this there was a drastic change in the dimensions of the tube near the fracture and it
looked like the materials of the tube got softened at an extreme rate. The evaluation as associated
with further confirming of the material softening and this evaluation was generally done upon the
bulk hardness that was observed near the location which failed. The values that were obtained was
seen to be exorbitantly law when compared with the materials that were investigated. Additionally
the earlier effect of the formation of the scale, and besides the softening was also responsible for
effecting the flow of the materials along with the creation of the bulge.
The inter-granular cracking along with the subsequent overloading of the ductile fracture under
excessive amount of hoop stress that was beyond the yield point of the tube material initially lead
to the failure at the time of exploitation of the service [10].
4. Solution
The most possible ways by which this kind of failures can be eliminated is by proper monitoring of
the entire process. Everything needs to be monitored in a proper way along with which proper
materials are also to be used of the purpose of creating a proper tube of the boilers which are essential
for the purpose of eliminating this kind of the problems. Besides this there is also a need of proper
cleaning as well so as to eliminate the formation of oxides as well as the subsequent spilling from
inside the tubes wall. Besides this good quality water should also be used so as to prevent thickening
of the walls [11]. Creep and softening of the materials is another problem that was responsible for the
failure. Oxide scale management would be helping in the smoothing of the heat transfer process
initially helping in the elimination of local overheating. Besides the steam pressure is to be decreased
at a substantial rate so as to decrease the stress occurring due to high temperature creep. This would
be helping in preventing the softening of the materials as well.
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5RISK MANAGEMENT
The SWOT analysis for the solution is as follows:
Strengths Weaknesses
Mitigate the uncertainties and
minimize the business risks
Estimate of oxide scale growth
into the super heater
Identification of product mix
and product market
Difficult to manage scale
exfoliation
Weak relationship to be existed for
range of oxidation
Not allowed to measure ultimate
shear strength of the interface
Opportunities Threats
Management of the wastes
which are generated by the hot
metal and steel
Develop phase field models for
describing the oxide scale
growth
Surface properties are affected by
growth of the oxide scale
Eliminate of potential
administration by 100% of the
nitrous oxide
The SWOT analysis for the solution is as follows:
Strengths Weaknesses
Mitigate the uncertainties and
minimize the business risks
Estimate of oxide scale growth
into the super heater
Identification of product mix
and product market
Difficult to manage scale
exfoliation
Weak relationship to be existed for
range of oxidation
Not allowed to measure ultimate
shear strength of the interface
Opportunities Threats
Management of the wastes
which are generated by the hot
metal and steel
Develop phase field models for
describing the oxide scale
growth
Surface properties are affected by
growth of the oxide scale
Eliminate of potential
administration by 100% of the
nitrous oxide
6RISK MANAGEMENT
5. References
[1.] French DN. Metallurgical failures in fossil fired boilers. second ed. New York: John Wiley &
Sons Inc.; 1993.
[2.] Purbolaksono J, Tarlochan F, Rahman MM, Nordin NF, Ahmad B. Failure investigation on
reheatertube due to deposit and wall thinning. J Fail Anal Prevent2009;9:365–9.
[3.] Parit AN, Tadamalle AP, Ramaswamy V. Failure investigation of secondary super heater
using CFD/CAE technique vol. 2. India: ESRSA publication; 2013. IJERT,ISSN: 2278–0181.
[4.] Kain V, Chandra K, Sharma BP. Failure of carbon steel tubes in a fluidized bed combustor.
Eng Fail Anal 2008;15:182–7.
[5.] Das G, Chowdhury SG, Ray AK, Das S, Bhattacharaya DK. Failure of a super heater tube.
Eng Fail Anal 2002;9:563–70.
[6.] Jones DRH. Engineering materials 3. London: Pergamon Press; 1993. p. 358.
[7.] Levy AV. Srinivasan V, Vedula K, editors. Corrosion and particle erosion at high
temperature. TMS; 1989. p. 207.
[8.] Levy AV. Solid particle erosion and erosion-corrosion of materials. Ohio: ASM International
Metals Park; 1995.
[9.] Liang Z, Jin X, Zhao Q. Investigation of overheating of the final super-heater in a 660 MW
power plant. Eng Fail Anal 2014;45:59–64.
[10.] Mukhopadhyay NK, Chowdhury SG, Das G, Chattoraj I, Das SK, Bhattacharya DK.
An investigation of the failure of low pressure steam turbine blades. Eng FailAnal
1998;5(3):181–93.
[11.] Rahman MM, Purbolaksono J, Ahmad J. Root cause failure analysis of a division
wall super heater tube of a coal-fired power station. Eng Fail Anal2010;17:1490–4.
5. References
[1.] French DN. Metallurgical failures in fossil fired boilers. second ed. New York: John Wiley &
Sons Inc.; 1993.
[2.] Purbolaksono J, Tarlochan F, Rahman MM, Nordin NF, Ahmad B. Failure investigation on
reheatertube due to deposit and wall thinning. J Fail Anal Prevent2009;9:365–9.
[3.] Parit AN, Tadamalle AP, Ramaswamy V. Failure investigation of secondary super heater
using CFD/CAE technique vol. 2. India: ESRSA publication; 2013. IJERT,ISSN: 2278–0181.
[4.] Kain V, Chandra K, Sharma BP. Failure of carbon steel tubes in a fluidized bed combustor.
Eng Fail Anal 2008;15:182–7.
[5.] Das G, Chowdhury SG, Ray AK, Das S, Bhattacharaya DK. Failure of a super heater tube.
Eng Fail Anal 2002;9:563–70.
[6.] Jones DRH. Engineering materials 3. London: Pergamon Press; 1993. p. 358.
[7.] Levy AV. Srinivasan V, Vedula K, editors. Corrosion and particle erosion at high
temperature. TMS; 1989. p. 207.
[8.] Levy AV. Solid particle erosion and erosion-corrosion of materials. Ohio: ASM International
Metals Park; 1995.
[9.] Liang Z, Jin X, Zhao Q. Investigation of overheating of the final super-heater in a 660 MW
power plant. Eng Fail Anal 2014;45:59–64.
[10.] Mukhopadhyay NK, Chowdhury SG, Das G, Chattoraj I, Das SK, Bhattacharya DK.
An investigation of the failure of low pressure steam turbine blades. Eng FailAnal
1998;5(3):181–93.
[11.] Rahman MM, Purbolaksono J, Ahmad J. Root cause failure analysis of a division
wall super heater tube of a coal-fired power station. Eng Fail Anal2010;17:1490–4.
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